00000101 愛(ài)普生技術(shù)資料 2017-5-4 7:24:13 很好,詳細(xì),只是英文看不懂 | 00010000 | 00010001 | 00010002 | 00010003 | 00010004 | 00010005 | 00010006 | 00010007 | 00010008 | 00010009 | 0001000A | 0001000C | 0001000F 愛(ài)普生技術(shù)資料 2017-5-4 7:24:13 很好,詳細(xì),只是英文看不懂 | 00010010 | 00010012 | 00010013 | 0001001B | 0001001D | 0001001E 愛(ài)普生技術(shù)資料 2017-5-4 7:24:13 很好,詳細(xì),只是英文看不懂 | 00010020 | 00010022 | 00010023 | 00010025 | 00010026 | 00010028 | 00010029 | 0001002A | 0001002B | 0001002D | 0001002F 愛(ài)普生技術(shù)資料 2017-5-4 7:24:13 很好,詳細(xì),只是英文看不懂 | 00010030 | 00010031 | 00010032 | 00010033 | 00010034 | 00010035 | 00010036 | 00010037 | 00010038 | 00010039 | 0001003A | 0001003B | 0001003C | 0001003D 愛(ài)普生技術(shù)資料 2017-5-4 7:24:13 很好,詳細(xì),只是英文看不懂 | 00020000 | 00020002 | 00020003 | 00020009 | 0002000A | 0002000B 愛(ài)普生技術(shù)資料 2017-5-4 7:24:13 很好,詳細(xì),只是英文看不懂 | 0003xxxx | 0Dxxxxxx | 0Exxxxxx 愛(ài)普生技術(shù)資料 2017-5-4 7:24:13 很好,詳細(xì),只是英文看不懂 | 100000E0 | 10000100 | 10000180 | 100001A0 | 100001C0 | 100005C0 | 10000xxx 愛(ài)普生技術(shù)資料 2017-5-4 7:24:13 很好,詳細(xì),只是英文看不懂 愛(ài)普生技術(shù)資料 2017-5-4 7:24:13 很好,詳細(xì),只是英文看不懂Source; Service Manual SP4400_4450_4800_4880_4880C_C ErrorCode; 00000101 Description; CR Motor life Explanation Indicates that the number of CR Motor passes has reached the specified value. The printer will develop the following problems and stop operation if printing is continued in this condition. ? Ink leakage through cracks in Ink Tube. ? Poor movement of Carriage Unit due to CR Motor internal wea Remedy 1. Check the number of times that the CR Motor has shuttled at “VIEWCOUNTER“ from Maintenance Mode 2, look for the measured number on the chart, and replace the corresponding parts. (Refer to Service Manual "1.4.6 Maintenance Mode 2" (p.90).) 2. The product-life cycle is the same as CR Motor-life cycle, so check and maintain all over the printer mechanism. Specially check points are shown below. ? Check for bending or damage to the Head FFC. ? Check for damage to the CR timing belt and PF timing belt. ? Check for abnormal noise when carriage unit moves (bearings are worn). ? Check for accumulation of paper dust or dust to paper feed route. If there is paper dust or dirt, refer to Service Manual 6.1.2 Important Maintenance Items During Service Operations (p.450) and carry out a cleaning. ? Refer to Chapter6 "Maintenance" (p.448), check the lubrication points, and lubricate them if they are dry. 3. Clear the CR Motor Life Counter. (Refer to Service Manual "5.6.4 Reset When CR Unit Change" (p.442).) TOP ErrorCode; 00010000 Description; PF Motor Encoder check error Explanation During initial operation at power on or during PF Motor operation, there may be a case where the encoder pulse signal can not be recognized at specified intervals. In such a case, this message is displayed and the printer stops operating. Cause of trouble ? Disconnected connector for the PF Encoder Sensor. ? Disconnected connector for the PF Motor. ? Broken wire for the PF Motor Encoder. ? Inverted wiring for A and B pulses. ? Inverted wiring for the PF Motor. ? PF Motor short ? PF Motor continuous excitation (voltage applied continuously, motor revolutions unusual) ? Broken power supply fuse for the PF motor driver (on the Main Board ) Points to be checked 1. The PF Encoder Sensor and the PF Loop Scale must be free from dust and dirt or any other foreign matters. 2. Execute encoder checking by the Service Manual "1.4.6.1 Self Testing Menu (SELF TESTING)" (p.91) in "Maintenance Mode 2". 3. The PF Timing Belt must be free from any defects and the belt must be in proper tension. 4. The PF Roller must rotate smoothly, free from undue load. 5. Measure the resistance value of the PF Motor (17.9 ± 15% [Ω]). If the PF Motor is found in short mode, replace the BOARD ASSY.,MAIN at the same time. 6. All the harness must be connected properly and free from short circuit or broken wire. Remedy 1. Check for dirt, paper dust or damage to the Loop Scale 2. Connect the PF Encoder Sensor connector or PF Motor connector. 3. PF Timing Belt Tension Adjustment (Service Manual p.378) 4. Replace the PF Encoder Sensor (p.357) 5. Replace the Motor Assy., PF (p.349) 6. Replace the C593 MAIN Board (p.226) TOP ErrorCode; 00010001 Description; PF Motor out of step Explanation During PF Motor operation, there may be a case where the encoder pulse signal within the specified range is not input within a specified period of time or the pulse width is extremely long or short. In such a case, the PF Motor is judged to be out-of-step, so that this message is displayed and the printer stops operating. Points to be checked 1. The PF Encoder Sensor and the PF Loop Scale must be free from dust and dirt or any other foreign matters. 2. Execute encoder checking by the Service Manual "1.4.6.1 Self Testing Menu (SELF TESTING)" (p.91) in "Maintenance Mode 2". 3. The PF Timing Belt must be free from any defects and the belt must be in proper tension. 4. The PF Roller must rotate smoothly, free from undue load. 5. Measure the resistance value of the PF Motor (17.9 ± 15% [Ω]). If the PF Motor is found in short mode, replace the BOARD ASSY.,MAIN at the same time. 6. All the harness must be connected properly and free from short circuit or broken wire. Remedy 1. Check for dirt, paper dust or damage to the Loop Scale. 2. Perform the PF Timing Belt Tension Adjustment (Service Manual p.378) 3. Replace the PF Encoder Sensor (p.357) 4. Replace the Motor Assy., PF (p.349) 5. Replace the C593 MAIN Board (p.226) TOP ErrorCode; 00010002 Description; PF Motor over current Explanation During PF Motor operation, there may be a case where an abnormal current out of the specified limits is detected in the PF Motor drive circuit on the BOARD ASSY., MAIN or a current exceeding the specified value is required. In such a case, this message is displayed and the printer stops operating. Points to be checked 1. The PF Loop Scale must be free from dust and dirt or any other foreign matters. 2. Measure the resistance value of the PF Motor (17.9 ± 15% [Ω]). If the PF Motor is found in short mode, replace the BOARD ASSY.,MAIN at the same time 3. By visual inspection, check the harness of the PF Motor for any problem causing a short circuit to the frame. Remedy 1. Check for dirt, paper dust or damage to the Loop Scale. 2. Replace the Motor Assy., PF (Service Manual p.349) 3. Replace the C593 MAIN Board (p.226) TOP ErrorCode; 00010003 Description; PF Motor in-position time-out Explanation At PF stop processing in PF Motor control, there may be a case where the paper can not move to the final target position within a specified period of time. In such a case, this message is displayed and the printer stops operating. Points to be checked 1. The PF Encoder Sensor and the PF Loop Scale must be free from dust and dirt or any other foreign matters. 2. Execute encoder checking by the Service Manual "1.4.6.1 Self Testing Menu (SELF TESTING)" (p.91) in "Maintenance Mode 2". 3. The PF Timing Belt must be free from any defects and the belt must be in proper tension. 4. The PF Roller must rotate smoothly, free from undue load. 5. Measure the resistance value of the PF Motor (17.9 ± 15% [Ω]). If the PF Motor is found in short mode, replace the BOARD ASSY.,MAIN at the same time. 6. All the harness must be connected properly and free from short circuit or broken wire. Remedy 1. Check for dirt, paper dust or damage to the Loop Scale. 2. Perform the PF Timing Belt Tension Adjustment (Service Manual p.378) 3. Replace the PF Encoder Sensor (p.357) 4. Replace the Motor Assy., PF (p.349) 5. Replace the C593 MAIN Board (p.226) TOP ErrorCode; 00010004 Description; CR Motor Encoder check error Explanation During initial operation at power on or during CR Motor operation, there may be a case where the encoder pulse signal is not input at specified intervals. In such a case, this message is displayed and the printer stops operating. Cause of trouble ? Disconnected FFC for the CR Encoder Sensor. ? Disconnected connector for the CR Motor. ? Broken wire for the CR Motor Encoder Sensor. ? Inverted wiring for A and B pulses. ? Inverted wiring for the CR Motor. ? CR Motor short ? Broken power supply fuse for the PF motor driver (on the Main Board ) Points to be checked 1. CR Scale is disconnected from CR Encoder Sensor. 2. The CR Encoder Sensor and the CR Scale must be free from dust and dirt or any other foreign matters. 3. Execute encoder checking by the Service Manual " 1.4.6.1 Self Testing Menu (SELF TESTING)" (p.91) in "Maintenance Mode 2". 4. The CR Timing Belt must be free from any defects and the belt must be in proper tension. 5. The Carriage Unit must slide smoothly, free from undue load. 6. Measure the resistance value of the CR Motor. (17.9 ± 10% [Ω]) 7. All the harness must be connected properly and free from short circuit or broken wire. Remedy 1. Check to see if the CR Scale for detection of the encoder pulse is removed. 2. Check for dirt, paper dust or damage to the CR Scale. 3. Check if connection of the CR Encoder Sensor connector or Motor Assy., CR connector. 4. Perform the CR Timing Belt Tension Adjustment (Service Manual p.376) 5. Replace the CR Encoder Sensor (p.280) 6. Replace the Motor Assy., CR (p.270) 7. Replace the C593 MAIN Board (p.226) TOP ErrorCode; 00010005 Description; CR Motor out of step Explanation During CR Motor operation, there may be a case where the encoder pulse signal within the specified range is not input within a specified period of time or the pulse width is extremely long or short. In such a case, the CR Motor is judged to be out-of-step, so that this message is displayed and the printer stops operating. Cause of trouble ? Defective CR Motor. ? CR Motor driver damage (42V system short) ? Broken temperature fuse for Cutter Solenoid. Points to be checked 1. CR Scale is disconnected from CR Encoder Sensor. 2. The CR Encoder and the CR scale must be free from dust and dirt or any other foreign matters. 3. Execute encoder checking by the Service Manual "1.4.6.1 Self Testing Menu (SELF TESTING)" (p.91) in "Maintenance Mode 2". 4. The CR Timing Belt must be free from any defects and the belt must be in proper tension. 5. Execute the CR_hp Sensor checking by the "1.4.6.1 Self TestingMenu (SELF TESTING)" (p.91) in "Maintenance Mode 2". 6. The Carriage Unit must slide smoothly, free from undue load. 7. Measure the resistance value of the CR Motor. (17.9 ± 10% [Ω]) 8. All the harness must be connected properly and free from short circuit or broken wire. Remedy 1. Check to see if the CR Scale for detection of the encoder pulse is removed 2. Check for dirt, paper dust or damage to the CR Scale. 3. Perform the CR Timing Belt Tension Adjustment (Service Manual p.376) 4. Replace the CR Encoder Sensor (p.280) 5. Replace the CR_hp Sensor (p.276) 6. Replace the Motor Assy., CR (p.270) 7. Replace the C593 MAIN Board (p.226) 8. Replace the Cutter Solenoid. TOP ErrorCode; 00010006 Description; CR Motor over current Explanation During CR Motor operation, there may be a case where an abnormal current out of the specified limits is detected in the CR Motor drive circuit on the BOARD ASSY., MAIN or a current exceeding the specified value is required. In such a case, this message is displayed and the printer stops operating. Points to be checked 1. The CR Scale must be free from dust and dirt or any other foreign matters. 2. Execute the CR_hp Sensor checking by the Service Manual "1.4.6.1 Self Testing Menu (SELF TESTING)" (p.91) in "Maintenance Mode 2". 3. Measure the resistance value of the CR Motor. (19.3± 10% [Ω]) If the CR Motor is found in short mode, replace the BOARD ASSY., MAIN at the same time. 4. By visual inspection, check the harness of the CR Motor for any problem causing a short circuit to the frame. Remedy 1. Check for dirt, paper dust or damage to the CR Scale. 2. Perform the CR Timing Belt Tension Adjustment (Service Manual p.376) 3. Replace the CR_hp Sensor (p.276) 4. Replace the Motor Assy., CR (p.270) 5. Replace the C593 MAIN Board (p.226) TOP ErrorCode; 00010007 Description; CR Motor in-position time-out Explanation At Carriage Unit stop processing in CR Motor control, there may be a case where the Carriage Unit can not move to the final target position within a specified period of time (as per pulse detection). In such a case, this message is displayed and the printer stops operating. Cause of trouble There are pulses smaller than out-of-step pulse remaining without completing paper feed. Points to be checked 1. CR Scale is not removed from CR Encoder Sensor. 2. The CR Encoder Sensor and the CR Scale must be free from dust and dirt or any other foreign matters. 3. Execute encoder checking by the Service Manual "1.4.6.1 Self Testing Menu (SELF TESTING)" (p.91) in "Maintenance Mode 2". 4. The CR Timing Belt must be free from any defects and the belt must be in proper tension. 5. The Carriage Unit must slide smoothly, free from undue load. 6. Measure the resistance value of the CR Motor. (19.3 ± 10% [Ω]) 7. All the harness must be connected properly and free from short circuit or broken wire. Remedy 1. Check to see if the CR Scale for detection of the encoder pulse is removed. 2. Check for dirt, paper dust or damage to the CR Scale. 3. Perform the CR Timing Belt Tension Adjustment (Service Manual p.376) 4. Replace the CR Encoder Sensor (p.280) 5. Replace the CR_hp Sensor (p.276) 6. Replace the Motor Assy., CR (p.270) 7. Replace the C593 MAIN Board (p.226) TOP ErrorCode; 00010008 Description; Servo interrupt watchdog time-out Explanation During the CR Motor or PF Motor operation, there may be a case where watch dog time-out is detected in the DC motor control circuit or on the ASIC. In such a case, this message is displayed and the printer stops operating. Remedy Since the cause is deemed to be a defective CPU or ASIC, replace the C593 MAIN Board (Service Manual p.226). TOP ErrorCode; 00010009 Description; System interrupt watchdog time-out Explanation In the data processing stage on the BOARD ASSY., MAIN, there may be a case where runaway or defective cash occurs on CPU or ASIC. In such a case, this message is displayed and the printer stops operating. Remedy If not cleared by turning the power OFF and back ON, the CPU or ASIC is deemed defective, so replace the C593 MAIN Board (Service Manual p.226). TOP 愛(ài)普生技術(shù)資料 2017-5-4 7:24:13 很好,詳細(xì),只是英文看不懂9, 熱門(mén)圖文
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